Monday, May 10, 2010

May 2010 Work Weekend

The weather was our enemy this weekend. Leading up the May work weekend, it had been unseasonably warm, summerlike if you will.

Thunderstorms passed through the area on Thursday night leaving low clouds and lingering rain on Friday. Saturday was dry but low clouds and a strong north wind made the 50F weather much more uncomfortable than expected.

The staff started to assemble Friday afternoon. At the same time, the 6's boiler was making its way back to the shop. Board member Dave O. had fetched it from the boiler maker a few days prior and kept it at his property near Des Moines.

Unfortunately, while awaiting pickup from the boilermaker and while sitting on his property, the unprotected shell gained a good coat of rust.

While this blog entry seems to be of the same voice used in nearly every other blog entry, we are all very excited that the 6's boiler is back at the shop. The boiler-less 6's chassis has been a constant reminder of how dear this steam locomotive is to our railroad and to our fans. Everyone at the MCRR is anxious to get the 6 running under its own power by this summer's Old Threshers' Reunion.

And in case the return of the boiler has our readers as excited as we are, we still need $$$ to get the 6 moving under its own power. Please go to our "Fix the Six" fundraising program page and make a donation!

The next few pictures show the boiler on Dave's trailer awaiting sandblasting.



























If you look closely, there is something written on the boiler, just above the trailer's two wheels.













One of the MCRR staff that installed the flues is the primary member of the "Shay Racing Team." He couldn't resist autographing the boiler. The history of the Shay Racing Team goes back a few years and was started as a friendly rivalry between engine crews. Oddly, every Shay RT member is also a member of the 6 cab crew and vice versa. While all crews operate all engines, many have their favorite!













This picture is from inside the firebox looking at its flue sheet. The sheet is shiny due to the old flues being welded in place, typical for an oil fired boiler. The welds and flue ends had to be ground off to install the new flues. The grinding was a job nobody wanted to do. After the flues were "swedged" in place, the boilermaker seal-welded the the flues.













Besides having the stays replaced, the stays supporting the firebox's crown sheet were converted to "flexible stays." While this author is rather clueless about why or how they are flexible, the odd looking protrusions -- sockets -- are characteristic of flexible stays.













Griffin W. is moving a pallet of sandblasting media close to the industrial sized sand blasting tool.













The gasoline air compressor is always finicky in the morning.













With the air compressor finally running, Dave O. starts the sand blasting. The two masked items (covered in pink tape) are the throttle linkage and the "stamp" which indicates the boiler maker's certification of the boiler.



























Volunteer Randy V. tinkers with the sand blaster's hopper and media outlet valve.













The sand blasting took most of the afternoon to complete. Once it was complete, it was moved into the shop and then coated with an aluminized high temperature primer giving it this lovely silver sheen.













Yes, that insignia is "Hello Kitty." (Note: The "Hello Kitty" image and all Sanrio characters are registered trademarks of Sanrio Co., Ltd. ("Sanrio"), and the images are copyrighted by Sanrio. Use of the "Hello Kitty" image is granted via the "terms of use" agreement found at www.sanrio.com)



























While others were sandblasting the 6's boiler, another work crew was tending to the "Quinn Coach." After being pulled around the track for so many years, some remedial maintenance was necessary. The two primary order's of business were to tighten the truss rods and to remove the interior in anticipation of having the floor refinished.













In order to tighten the truss rods, additional threads had to be made on the rod ends. Previously, washers had been added every few years as the coach was heavily utilized at the three big operating events.

MCRR volunteers Ken C. (right) and Elliot H. use a pair of combination wrenches to turn the die on the truss rod ends. With only a 1/4 turn stroke at a time, adding 1.5 inches of extra thread took some time.



























With the new threads cut, Griffin W. reinforces the steps.













Master craftsman John W. cleans one of the coach's lamps.













MCRR Conductor Steve R. pauses for the camera while washing the wood interior of the coach.













Bill F. washes the woodwork with "Murphy's Oil Soap." The years of service added a massive layer of dirt to the wood work. We were all surprised on how much brighter the walls and ceiling appeared after a thorough washing.













That's Dillon W. coming through the door in the background.













Reinforcing the steps required extra long bolts. Shelby G. discusses Dustin B's welding handiwork.













FNG Dallas K. applies some black paint to the end sill where the step reinforcements and truss rod ends had been modified.













With the work done, volunteers Brian B., FNG Dallas K., and Paul K chat about the day's accomplishments.













-steam.airman

Monday, April 19, 2010

April 2010 Work Weekend

The work weekend started a few days early for a few of the MCRR volunteers.

While awaiting the 6's boiler, numerous hours have been invested in the D-9. If you scan through the previous blog entries you will see what progress has been made.

To summarize what has transpired, starting about this time last year, the sheet metal and various parts surrounding the engine and torque converter were removed. During the summer of 2009, the engine/TC was removed and the innards of the torque converter were placed into the new crack-free housing. During the 2009 Old Threshers' Reunion, when the engine/TC was installed and tested, another leak was discovered that, unfortunately, requires R&R of the engine/TC unit. (Plans are afoot to repair that leak; we should see the D-9 moving under its own power fairly soon.) Meanwhile, an idle volunteer sandblasted nearly all the loose D-9 parts and others started the paint removal and refurbishment of the cab. In November, 2009, the loose parts were primed. During the last few months, the rotted sheet metal on the cab has been replaced and the installation of a train brake system was started.

So what happened to it this month? The cab repairs were completed and the air brake system was completed. Plus..."Bad Kitty" attacked, as shown here, leaving her signature portrait on the sides and rear of the engine!













As one might expect, tinkering with the air brakes didn't require the expertise of everyone, so other things did occur.

A large number of conductors and ticket sales personnel met Saturday morning to clean the 2009 North Pole Express remnants out of the South Station and the coaches. The next few pictures show the coaches being from Museum B and the South Station to a spot outside the South Station. This gave the staff plenty of light to see what needed cleaning and repair.

No pictures or details of exactly what was accomplished at or around the South Station can be given here; this reporter was busy in the shop (and fooling around at the Mt Pleasant airport!) and was unable to document what was happening "over there." Perhaps someone with the coaches was taking pictures and can supply them and text for me to insert into this blog entry.



















































































Outside the shop, along the mainline tracks west of the road, a group of volunteers corrected a long-forming problem: the rails had developed a negative camber, with the outside rail lower than the inside rail.

What should have been a "quick" project turned out to last long after nightfall. Besides needing to jack the ties and rails, a large number of ties needed to be replaced.

Replacing (spotting) ties has been made much easier than ever before with the special bucket on the Case backhoe. The bucket is exactly the width of a tie and with two strokes the old tie is knocked out and a new tie pushed into place. Contrast that with using the skid-steer, chains, and tie-tongs!

The next bunch of pictures show the staff moving the ties about, spiking the rails to the ties, and tamping the ballast into place.

Long time volunteer Chris C is shown using the pneumatic ballast tamper in the next two photos.



























Volunteer John W holds up a shovel as the others do all the work.













Griffin walks between the matt-tractor loaded with ties and ties laying on the ground.













John W holds a rail in place while Griffin moves some ballast out of the trench where the new tie will be tucked into place.













Trying to decide what happens next.













The special bucket is clearly shown on the Case backhoe. The bucket has an official railroad name but I haven't a clue what it might be.













Dustin B and Chris C watch as Griffin skillfully moves a tie under the rail with the Case backhoe.













That's Griffin carefully manipulating the controls of the Case backhoe.













Brian B (squatting) and Dustin B watch intently as Chris C pries the end of the tie in place.













A few more nudges with the bucket and the tie is ready for spiking.













Dustin B taps the tie plate square with the tie before spiking.













Dustin B has a few words with the Case backhoe operator.













Brian B lifts the rail so Dustin can get the tie plate under the rail.



























The Plymouth switcher 14 basks in the sun.













John W, Jerry C, Lindsay R and Lindsay's aunt (yikes! her name escapes me at this second!) chit chat outside the South Station.













Back at the track project, Chris C pounds a spike into place.













Apparently untrustworthy with a large hammer, Brian B starts a spike in the tie with a tiny hammer.













Chris C uses a pneumatic ballast tamper to pound the material under the tie.













As the tamper pushes ballast under the tie, additional ballast must be shoveled into the hollowed out space. Each tamper operator requires the full time service of a ballast shovel operator.













His work complete at the South Station, John W walks to the track project site.













Director Dave R pilots the fork lift back into the shop.













-steam.airman